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for the 2010 season
click here |
for the 2009 season
click here |
for the 2008 season
click here |
for the 2007
season
click here |
for the 2006
season
click here |
for the 2005 season
click here |
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Empire 9/25/11 Test
And
2011 Season Recap
Saturday 9/24/11 the car went back together.
Sunday we went to Empire Dragway to test before heading to our last race
in Indy the following weekend. We set up our pit area, put the car up on
the stands and started it up to warm it up. Steve noticed a small fuel
leak and told me to shut it down. He determined that the fuel leak was
coming from the intake gasket area. So to fix it we needed to take off the
supercharger and the manifold. Lucky for me we were able to find a couple
of volunteers to help. Bill and Bill – Thanks guys you saved me a lot of
work. We got the fuel leak fixed, put everything back together, and
started it up. The warm up went well so we went to the lanes to make a
run.
The run did not go well – 9.135 and 90.71
mph – Steve got out of it early because he was getting that dreaded oil
bath. The RTV that Steve used to seal the intake manifold did not fully
set up, so under pressure it leaked. Then when we got back to the pits we
found that #1 and #3 had a problem. Once Steve got the valve cover off he
found that the bolts that hold the rocker arm stands broke off inside the
head. There is no way we can get that fixed in time to go to Indy. We are
done for the year.
That brings me to the season recap. This was
a so – so season. We had good and bad.
The good: We won two races (although the
first one there was only two cars in the class) we were runner up at the
NHRA Hot Rod Reunion. We were the fastest car at the NPCA race in Lyons,
IN but because of rain delays they called the race and split the purse. I
think that would have been another win for the SS3 race team.
The bad: We lost first round at three races.
We broke or had problems at 4 races. One was torque converter problems the
other three were burnt pistons.
We had two races called one due to rain
delays the other due to low car count.
The low car count was something we saw at
every event this year. There was not one event this year that we had a
full field, not even the NHRA Reunion at Bowling Green. I’m sure the
economy has much to do with this.
What makes me feel good about this season is
that the two events that had close to full class – NHRA Reunion and NDRL
at Edgewater – we did great. We were runner up at the first, and won the
second.
So if it wasn’t for all the damage we did
throughout the year, it really was a good season. That’s my story and I’m
sticking to it.
Our new rig was a big plus for the year.
What a super unit this is, I LOVE it. And it doesn’t stop with the race
season. I have made reservations at an RV park in Ft Myers, FL for January
15 thru March 15. We will attend the NDRL banquet in Indy in November.
After the banquet we will head to Florida. The rig will be stored until
January 15th then it will be put in an RV site. Then Steve and
I will fly down and stay in the Florida sunshine for two weeks. We will
stay for a couple weeks in February and a week in March, then head north –
with a stop in Gainesville for the Gatornationals – then home. That gets
us out of upstate NY during the winter for 5 weeks. That’s equates to 35
days of 3 to 6 inches per day of snow. I will not miss that.
Until next year, stay healthy, safe, warm
and think spring. |
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August 20, 2011 Quick 16
Empire Dragway
Leicester, NY
After leaving the Dunn Tire Quick 8 late Friday night we drove to
Leicester, NY and pulled into Empire Dragway late Friday, or should I say
early Saturday. We parked the Motorhome/trailer in our favorite spot –
looking down the strip, and went to bed.
The next day our qualifying runs were at
3:00 pm and 5:00 pm. so we had all morning to relax and get ready for
qualifying.
Our first qualifying run we ran 4.50 and 156
MPH, which is perfect for our 7.0 index racing, but not so good for a
Quick 16 event. We need to step it up. Steve made a pulley and fuel
changes.
The second run we ran 4.47 and 158 MPH,
which was better, except for we blew the blower belt off, and damaged the
#4 piston. We were done for the day.
As is ended up, we needed to replace the #4
piston, sleeve # 4 cylinder, and possibly make a head gasket change and
change the cam timing.
At this time we are going through everything
trying to find out just what is wrong. Why are we doing this constant
damage?
Our next race is not until the end of
September, at Indy. We need to find and correct this problem before that
race. |
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August 19, 2011 Quick 8
Dunn Tire Raceway Park
Lancaster, NY
On our schedule for this weekend was the NPCA Ohio Nostalgia Nationals II
at Kil-Kare Dragway in Xenia, OH, but because of all our damage problems
we decided last minute to go to two “Quick” events at local tracks. The
first was at Dunn Tire Raceway Park in Lancaster, NY on Friday 8/19/11.
This was a big one. They were paying $3,000.00 to win. With that kind of
money, you know that every high dollar, extremely fast car was going to be
there. We would be lucking just to qualify. This would be an eighth mile
race.
It was hot and humid, but because it was an
evening race it did cool down a bit before we ran. The first qualifying
run we were in the left lane, which is Steve’s lane of choice. The car
made an immediate right and took out the 60’ cone. This is very, very
unusual for our car. So we only ran a 6.47.
The second run we were in the right lane. We
ran a 4.51 and 154 mph which put us at the #5 qualifier. We made it in the
show.
The first round of eliminations we were up
against Grainy Brothers – a very tough team, but we have beaten them in
the past. They had lane choice, and chose the left lane. They ran 4.17 and
169 mph to our 4.55 and 135 mph – Steve had to shut things down after he
took out the MPH and ET cones at the top end of the drag strip. Again the
car was way out of control. This is very unusual. Steve checked things out
and determined that the “puke tank” was putting some oil down under the
slicks, which is why the car would not go A to B like it normally does.
So, this is another thing we need to fix.
Even with the first round loss, we got more
in winnings than we had to pay for entry fee, so it was not a total loss,
and it looks like we didn’t damage anything.
We left the track after 11:30pm and headed
to Empire at Leicester, NY. We were told that the gates were open there
and we could pull in and stay the night. |
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Edgewater Sports Park
NDRL Race
August 12-13, 2011
This was the final NDRL race of the season, and it was super with a
capital S. The car count was not stealer, but it was good – much better
than any other event we had attended. The track was in great shape and the
weather was better that the forecast. Now that does not mean that it was
perfect – it wasn’t – it was hot and humid – with bad air. But we didn’t
have the rain that was called for. We pulled out of the track at 11:00pm
on Saturday and it was just starting to rain – great timing.
There were 6 Pro 7.0 cars there – we
qualified #3 with a 7.33 and 180 mph.
Round 1 of Eliminations – we ran 7.30 to a
7.51 for the 1st round win.
Round 2 of Eliminations – we ran 7.14 to a
7.25 against Mike Sexton for the 2nd round win.
Round 3 & final we ran 7.21 to a 7.16 red
light against Ron Robinson for the final round win.
WE WON!!!
Finally, we won an event with a decent car
count and cars that are hard to beat!
This was the first year for the NDRL
(Nostalgia Drag Racing League). This group is very well organized,
although they did experience some “new group” issues. They are already
planning the races for 2012, and it looks like they will have 5 races next
year instead of 3. Their goal is to grow slowly so they don’t have those
“get too big to fast” issues.
Great job to all of you that made this
happen! We are looking forward to the 2012 season with the NDRL. |
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Dunn Raceway Park
Sunday Niagara Weekend
August 7, 2011
After the Q16 race at Empire we had to wait for the new pistons to arrive
so we didn’t make the July 30th NDRL race at Bowling Green, KY.
So here we are at the Niagara Reunion.
Mother Nature was not kind to us at this
event. We had lots of rain delays.
This was an eight mile event. We were the #3
qualifier @ 4.56. We had to run the #2 qualifier-Head Knocker @ 4.57. So
we were really, really close.
To make a long story short – We lost by
.0021 – a close drag race, but we were at the losing end. But it looks
like we didn’t break anything!! |
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Empire Dragway
Leicester, NY
July 16,
2011
Quick 16
Our schedule shows that we were going to the NQSA event at Lyons Raceway
Park on this date. But because of the damage we did at the last event we
decided to go to a local Quick 16 event at Empire Dragway in Leicester,
NY, which is only about one hour from our house. This was an eight mile
event. The weather was hot – 90+ degrees with a corrected altitude of
3400’.
We made 2 test runs – 4.66 & 155 mph and
4.54 and 158 mph. Then we made 2 qualifying runs – 4.52 & 156 mph. The
second run Steve went before the tree activated , so we didn’t get a time
slip.
But that didn’t matter because we burnt 4
more pistons. We were done!!!
We need to find out what is going on inside
this engine. |
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Pacemakers Dragway Park
Mt Vernon, OH
July 9, 2011
NPCA
This event was an NPCA race combined with the Ohio Mustang club and
the Pacemakers Dragway Park regular Saturday race. As it turned out, the
car count for all three was down – way down. There were only 4 NPCA cars
there. And they were all in different classes – so the track cancelled the
race. We were refunded our entry fee, and allowed to make as many time
trials as we wanted.
This was a GREAT track. We need to have
races at tracks like this.
The weather was great, 87 and sunny.
Corrected altitude was 3600 ft – not good air.
We made 1 test run. We ran 4.55 and 151 mph
(1/8 mile).
We didn’t know it at the time, but we burnt
2 pistons on that run.
So – we drove to Ohio to make one run – to
burn up 2 pistons – Not Good!!! |
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Dave Himes Nostalgia Nationals
The New Muncie Dragway
June 25, 2011
This is an NPCA (Nostalgia Pro Comp Assn) race. We have been at this track
twice before – both times were rained out. But this time the forecast is
great – temps in the high 70’s and no rain. We had company this race. Our
daughter Valerie and her two daughters Maris and McKenna went with us.
June 24th is Valerie’s and McKenna’s birthday so we packed an ice cream
cake in the freezer and set out for the track. We arrived at the track
about 4:00 pm on Friday the 24th. We set up our pit area, made dinner put
the candles on the ice cream cake, sang “Happy Birthday” and ate cake.
Other than that we watched race teams pull in. And pull in they did. The
pits were packed. But not with cars in our class. There were only two of
us. SS3 Race Team and the Mechanical Bull Team of Ronnie Robinson.
We went for a test run at noon on Saturday. We ran 7.017 and 192.43 mph,
Ronnie ran 7.115 and 187.81 mph. We were in the left lane, Ronnie was in
the right.
At 4:37 we had our qualifying run. This time we were in the right lane and
Ronnie was in the left. We ran a 7.100 and 190.67 mph, Ronnie ran 7.021
and 189.91 mph. Almost a complete switch from the previous run. So this
looks like the left lane is the better lane. Ronnie is the #1 qualifier –
so he puts us in the right lane.
We went up for the First round of eliminations – which is the only round
of eliminations – at 9:12 pm. We were told by Ronnie’s crew told us that
he would be doing a short burnout as he had some problems with his air
system. We ran 7.091 and 172.18 mph, Ronnie ran 7.275 and 184.53. We got
the Win. Valerie, Maris and McKenna were very excited. When there are only
two cars in the field it is kinda hard to get excited about the win, but
it was good for the girls. I felt bad for Ronnie and his crew – it sucks
to have mechanical problems.
The car count has been down at every event we have been to so far. I’m
sure that the cost of gas and diesel has a lot to do with this. I can only
hope that this gets better in the future.
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NHRA Hot Rod Reunion
Beech Bend Raceway Park, Bowling Green, KY
June 16 – 18, 2011
After our two and a half day stay in the Motorhome at Beech Bend
Campground we packed up Wednesday morning and made the approximately 2
tenths of a mile move over to the Pits at Beech Bend Raceway Park. We set
up our pit area and towed the car down to the end of the track for tech.
This was about a quarter of a mile away. When we left our trailer it was
sunny. As soon as we approached the line for tech it started to rain –
great big raindrops! We quickly covered the car and ducked under the roof
that covers the scale and time slip pickup booth. It rained for about five
minutes then quit. We finished with tech and went back to our pit spot. We
were not scheduled to make any runs on Wednesday, so we relaxed, walked
around and visited. Then we went into town with several other races for
dinner at Applebee’s. While we were in Applebee’s it poured but was pretty
much done by the time we left.
On Thursday we had one qualifying run scheduled. We went up for that run
right around 4 pm. It was hot and sunny. The corrected altitude was a
little over 3500 feet. Steve adjusted the tune up to adjust for the bad
air. We ran 7.12 and 185 mph. There were five other cars in our class.
Four of them ran in the 7.40’s and the other one went too fast, so we were
the #1 qualifier after round 1.
Friday we had two qualifying runs, one at 1:30 and one at 5 pm. It was
again hot and sunny with the same bad air. Qualifying run #2 we ran 7.107
and 189 mph and remained the #1 qualifier. Qualifying run #3 we ran 7.105
and 190 mph. Unfortunately a funny car from Oregon went 7.02 and took the
#1 spot away from us, so we ended up the #2 qualifier.
Saturday we woke up to very cloudy, mean looking skies. It didn’t take
long to start raining, and it continued for hours, sometimes very hard. It
finally quit around 3 pm and the track crew started drying the track.
While we waited we were visited by Dani Leigh aka “Squirt” and her Dad. If
you look back at my June of 2007 write up for the Indy Goodguys event, you
will see a picture of Dani sitting in our car, and you can read about how
much of a “Gear Head” she was, even at the age of four. Well now she is
eight and still a huge “Gear Head” and race fan. She told me about all the
Top Fuel and Funny car runs she had watched so far this weekend, she asked
a lot of questions – good questions, about the car and the data recorder.
This girl needs to be in a junior dragster!
We finally got to go up for our first round of eliminations at 7:10 pm.
The temps were cooler, and it was partly cloudy, so the air was somewhat
better than it was Thursday and Friday. We ran 7.139 and 189 mph for the
win. The second round was at 9:29 pm. We ran a 7:171 and 161 mph for the
win. You can tell that Steve let off before the finish on both runs. This
first run because the other driver went red. Steve saw that and knew he
had won the round. The second run he felt the car was on a “too fast” run.
He was way ahead and didn’t want to break out. The time slip showed that
he ran 4.49 at the eighth mile, so he was indeed too fast, and letting off
early was the wise thing to do. The final round was at 10:51 pm, against
the #1 qualifier – that funny car from Oregon. We ran 7.20 and 152 mph to
his 7.07 and 197 mph for the loss. Again Steve felt the car was too fast,
and again he was right. The eight mile time was 4.46 – he was going to
break out, so again letting off early was the right thing to do, but he
just did it a little too early.
So we were “runner Up’ for the second year in a row at this event. Oh well
it is better than going out first round, and there is always next year.
Steve went over to congratulate the winning team. They talked to him about
October NHRA Reunion that is held in Bakersfield CA. They will be there
and were trying to talk Steve into going. It’s a long haul, but maybe. We
will think about it.
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NPCA Nostalgia Nationals
Lyons Raceway Park, Lyons, IN
June 10 & 11, 2011
We arrived at Lyons Raceway Park at 4:30 pm
on Friday June 10th. The track was open for testing until 9:30
pm. We set up our pit area then watched a couple of the faster cars make a
run so we could see what the track was like. It didn’t look to terribly
bad, so we decided to make a run.
This is an eighth mile track so our index if
4.50. We made a run at 8:43 pm. The tires spun and then started to shake.
Steve pedaled it then short shifted and got it to settle down. It ended up
running a 4.661 and 155.74. The top end of the run was okay, but our 60’
time was 1.18 – it should be about 1.03.
Saturday we were scheduled to have two
qualifying runs, starting at 3:00 pm. But the Saturday morning rain caused
some delays, so our first run was at 5:39 pm. The temps were in the mid
80’s and it was humid so the corrected altitude was 3191 – not good air,
but Steve thought he had the correct tune up. We ran 4.549 and 155.44.
This put us in the #1 qualifying spot. Our second run was at 6:57 pm. The
air was starting to get a little better, but not much so Steve left the
tune up alone. We ran 4.487 and 155.15 – so we were a little too fast, but
we held on to that #1 spot. There were 5 cars in our class so that #1
gives us a bye run first round.
Then it started to rain! It finally quit
raining about 10 pm and they started drying the track.
We made our 1st round of
eliminations at 12:21 am. At that time the temp was 75 and the corrected
altitude was 2445 – much better air, but the dew was starting to cover
everything. Steve had changed the pulley and adjusted the fuel. We had
that bye run so it didn’t matter if he went too fast or way too slow. We
ran 4.481 and 154.21 – Okay we need to slow it down a little more. Of the
five cars in our class we were the only one that went straight down the
track. The dew was starting to cause some problems.
Because of the safety issue the track
personnel decided to not run the faster cars (us) and instead they split
the purse between the three remaining cars. This was okay with all of us.
If they had us continue we would have been racing until 3:00 am, and
someone might have damaged their car and gotten hurt. We packed up and
went to bed.
The next morning we headed to Bowling Green,
KY.
We have the Motorhome in the campground next
to the track at Beech Bend Raceway Park until Wednesday, 6/15 morning when
we move over to the pit area, set up and get ready for the NHRA Hot Rod
Reunion. |
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Empire Dragway
Test ‘n Tune
May 25th & June 3rd, 2011
Finally Mother Nature gave us and track
owner Bob Metcalf a break! On Wednesday 5/25/11 we took the bantam to our
local track for test ‘n tune. We need to know if our torque converter
problems are over. The temps are in the low 70’s with high humidity and a
corrected altitude of 2500+. Not great air, but all we need is some data.
We went up for our first test at 7:08 pm. We
ran a 7.23 and 184.08 mph with a 1.07 60’ time. Steve had backed down the
tune up to pre INDY race because he knew that all the INDY race data
didn’t mean anything due to the torque converter issues, so this run was
right where we thought it would be. Okay, now we are making progress. The
only problem with this run was the data we got. Our data recorder stopped
recording at 4+ seconds, which means we only got data for a little only
half the run – not good but not terrible either. I really didn’t know what
was going on with the data recorder, so I enlisted a little help from a
local “geek” Paul. He helped me reset some settings and we were good to go
for the second test run. The next run Steve had a bye run. He staged the
car, but then it went thru the lights. They backed him up and waited for
the lights to reset, then re-staged him. He ran a 7.09 and 186.57 mph with
a 1.04 60’ time. This is right where we need to be. The only problem with
the run was the data. When they backed him up, it started the data
recorder. By the time the lights reset and the run started, the data
recorder timed out – so we didn’t get any data for that run. The data
would have been a huge plus, but just seeing that 60’ time of 1.04 told us
that the torque converter issue was no longer an issue.
On Friday June 3rd we again had a
decent weather day in upstate NY, so we headed to our local track – Empire
Dragway.
We made two test runs. The first run was at
6:57 pm. The corrected altitude was 2300. We ran a 6.98 and 191.04 mph
with a 1.05 60’ time. All looks good. When I download the data I see that
the EGT’s are on the low side, which means the tune up is on the “fat”
side. This shows us that we can go even faster without doing damage. Keep
in mind that for our nostalgia racing we need to run 7.0. So we don’t have
to go faster than this run – we need to slow it down.
We went up for the second test run. We ran a
6.96 and 190.03 mph. Again the EGT’s are low. Again, all looks good. We
are good to go for the next NPCA race in Lyons, IN June 11th |
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Nostalgia Drag Racing League
Lucas Oil Raceway, Indianapolis, IN
May 7 & 8, 2011
A whole lot of “firsts” here. This was the
first race for the Nostalgia Drag Racing League. This was the first race
with the 477 Arias engine in the Bantam. This was the first race with the
new Rig. The only “first” that didn’t happen was we didn’t come in first.
Because of the incredibly wet spring our
local track did not open, so we headed to Indy with an untested car.
Friday the 6th the track was open for test ‘n tune so we made
three runs. The car was terribly SLOW. First run we went 9.26 and 105.41
mph. Steve made some changes and we tried again. This time we ran 8.08 and
172.14 mph. Steve made more changes. The last run we ran 8.06 and 172.94
mph. We were getting nowhere – fast. Steve said the car felt just like
when we had the bad sprag in the torque converter a few years ago. So, the
car went into the trailer and we started taking it apart to get the torque
converter out. We only worked on it for an hour or so, then quit for the
night. Early next morning we were back at it. It started to rain and the
track called it a day. Qualifying and Eliminations would both be done on
Sunday. The rain worked in our favor. We needed the time to work on the
car. Steve got the torque converter apart and it was apparent that there
was a problem. The new stator that Steve had put in over the winter was
chewed up all around the edge. He put the old stator back in and closed up
the converter and reassembled the car. We started it up and drove around
the pit area. Steve said that it felt like it had a lot more power.
Sunday morning we woke up to fog and a fine
misty rain. By 10:00 am it was over, and at 1:00 we made our first
qualifying run. We ran 7.84 and 177.28 mph. Still a long way from our 7.00
index. Every run so far, our 60’ times were way off. We usually do about
1.04 but the best we good do now was 1.23. Steve made some changes to the
engine tune up and also to the launch control – trying to improve that 60’
time and we went up for our second attempt. We ran 7.59 and 183.05 mph –
better but not good. Again the 60’ time was 1.23. The car just could not
get going. Even with the slow, slow runs we ended up the #4 qualifier,
only because a few cars went too fast and broke out. Steve made some more
changes and we went for the first round of Eliminations, which was also
our last round of eliminations. We ran a 7.55 and 185.41 mph with another
1.23 60’ time.
Of course Steve thought about this all the
way home. By the time we got home he was convinced that the torque
converter was still the problem. He started thinking that the sprag must
be in wrong. The car went into the shop and the converter came back out.
Sure enough, he had the sprag in backwards. So we had a torque absorber
instead of a torque multiplier. No wonder the car couldn’t get out of its
own way!
The April 16th race at Music City
Raceway in Tennessee, and the May 21st race in Bowling Green,
Kentucky were both rained out, so we only attended one race with the bad
converter. Now we just need to get to the local track before the June 11th
race in Lyons, IN to make sure we have our problems solved. |
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