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for the 2007 season
click here |
for the 2006 season
click here |
for the 2005 season
click here |
last edited
11/29/2008
2008 Schedule of
Events
May 17 - Match Race Mania, Route 66 Raceway, Joliet IL
May 31 - June 1 - Muscle Car Madness, Gateway Intl Raceway, Madison IL
June 6 - 8 - Goodguys Indy, Indianapolis IN, NPCA Points Race
June 13 - 15 - NHRA Hot Rod Reunion, Bowling Green, KY
August 1 - 3 - Niagara Reunion, Willys Home Run, Lancaster NY
August 9 - Night of Fire, Muncie Dragway, Muncie, IN
August 22 - 24 - Nitro Blast '08, Midstate Dragway, Havana IL
September 5 - 7 - Goodguys Blue Swede Cruise, Norwalk OH, NPCA Points Race
September 20 - Match Race Mania II, Muncie Dragway, Muncie IN
October 3 - 5 - Muscle Car Madness, Kansas City Raceway, KC, MO, NPCA Points
Race
October 17 - 19 - Goodguys Nostalgia Nationals, Bowling Green KY, NPCA Points
Race
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SS3 Race Team
2008 Season Recap |
We attended 8 Nostalgia Events this year. We started the season with an
8-71 supercharger and competed in the Pro Comp II class, which has a 7.50
index. Then we went to a 14-71 supercharger and competed in the Pro Comp I
class, with a 7.00 index. Until the October event in Kansas City where the
14-71 supercharger self destructed (nothing that Fowlers Engines Inc. and
our credit card couldn’t fix). Then we finished the season with the 10-71
supercharger (we put that on in the pits at Kansas City) and went back to
the Pro Comp II class for the final event of the season.
We battled with rain at three events – only one was rained out. We battled
with the tree at 3 events - that dreaded Red bulb sending us to the
trailer. And we had numerous mechanical problems at the Kansas City event.
We were the #1 qualifier and won the Niagara Reunion in Lancaster, NY.
This was so great because this is the only event in New York State, and is
only 60 miles from our house. A great many of our family members and
friends were there to see our victory.
We finished 5th in the points in Pro Comp I and 4th in the points in Pro
Comp II.
Win, lose or rained out, we enjoyed every event. For the most part the car
ran good and we made progress on the tune up. But the best part of racing
in the Nostalgia Pro Comp Association is the people. We play jokes on each
other, drink, eat and laugh when we’re not racing, and help each other out
when we are racing – remember that “crew chief orgy” in Kansas City?
Steve has the car in the garage and apart for routine maintenance . The
14-71 supercharger is back from Fowlers. That will go back on the car and
we will go back to the Pro Comp I class for 2009.
Thanks again to our sponsor Specialty Tools Inc. for their support. Please
visit their website – just click on their logo that is on our home page.
It’s going to be a long cold winter. I can’t wait to see everyone at the
track next spring. Until then be happy, healthy, stay safe and THINK
SPRING!!
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1st Annual
Goodguys Nostalgia Nationals
Beech Bend Raceway, Bowling Green, KY
October 17-19, 2008 |
We flew back to Indy on Thursday October 16th. The flight was
on time, so we were at Jeff Lawson’s shop to pick up the trailer by 11:00
am. While Jeff had possession of our car and trailer he did some repair
work for us. Among all the over problems we had at Kansas City, we also
had a small crack in the rear end housing. Steve tried to seal it up with
epoxy and it worked while the car was sitting in the pits, but as soon as
it made a run, the twisting action of the launch would open the crack, and
the dripping of oil would start again. We can’t thank you enough Jeff.
We were on our way to
Beech Bend Raceway at 11:45 am. It rained on and off for the entire 4
hour trip to Bowling Green. We arrived at the track right around 3:00 pm
(central time). Again, we had on and off rain, but nothing that
interfered with setting up our pit area and socializing with our fellow
NPCA racers.
We had two qualifying runs scheduled for Friday, and two on Saturday.
Eliminations would be on Sunday. Our first qualifying run the car ran
7.42 and 167 mph – just a little to fast (we are running in the 7.50 class
this race). Steve made a pulley change, and the car ran 7.65 and 166 mph
on the second run. He slowed it down a little too much! The fuel
pressure was just a tad low, so Steve changed the nozzles to see if he
could pick that up a little, and lean it out a little. The first run on
Saturday the car improved to a 7.62 and 167 mph. Steve again made some
nozzle changes. The second run was 7.56 and 167 mph. Now were getting
close! We ended up in the number 3 qualifying position.
We won the first round with a 7.78 and 128 mph run. Steve was afraid that
he might go to fast because the air was so good – the corrected altitude
was only at 630 feet above sea level. Steve was so far ahead of the guy
at the eight mile he let off. Before the second round Steve said that
he was going to concentrate on the tree, and cut a good light. I hate it
when he says that! The car ran a 7.53 and 165 mph – our best run so far
with the 10/71 supercharger. But!!! He went .001 RED! One one-thousand
of a second to soon. So, we were done.
After the rain on Thursday, the weather was absolutely perfect. Sunny and
mid to high 70’s all three days. We had a great time with all our NPCA
buddies at the beautiful Beech Bend Raceway Park. Even with the red light
loss, it was a wonderful end to the 2008 season.
On the way home, we stopped at
Fowler Engines in Columbus Ohio to drop off the damaged 14/71
supercharger for repair, and the 10/71 supercharger for freshening.
In November I will post a 2008 season recap, and a tentative 2009 schedule
– based on the limited info we have at this time.
Please check out the
website of our sponsor
Specialty Tools, by clicking on their logo that is on our home page.
And check out the Photo and
Video pages of our site. |
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Muscle Car Reunion
Kansas City International Raceway
October 3 – 5, 2008 |
It’s
a long haul to KCIR – 1050 miles – a 17 hour drive. The good news is that
we had no problems during that 17 hour drive, and the weather was perfect
– mid seventies and sunny the entire weekend. The bad news is that
everything that could go wrong during the race part of the weekend did go
wrong.
When we left Norwalk last month the car was running great. After we got
home Steve did some maintenance - changed the oil, and adjusted the relief
valve on the oil pump to boost the oil pressure.
Friday afternoon at KCIR we had a time trial at 2:00. An hour before, we
started the car to warm it up. We only had 40 lbs of oil pressure – we
should have had 90 to 100 lbs. We drained the oil, took off the oil pan
(during this I managed to drop not one, but two of the oil pan bolts into
the pan of drained oil) and took off the oil pump. Steve took apart the
oil pump- found that the relief value was stuck. He fixed it and put it
back together again. We put the pump back on the car, put the oil pan back
on, filled it with oil and started the car. We now had 95 lbs of oil
pressure. Of course we had missed the 2:00 time trial, but we were ready
to go for the first qualifying run at 7:00 pm. We went up for the run,
Steve did the burnout, but took a long time to back up and stage the car.
I didn’t know it at the time, but he was having trouble with the trans
brake button, which he has to hold down to back up the car – it kept
popping off. Then when he staged the car, the trans brake did not hold, so
that messed up the launch of the car, and then it didn’t shift, so Steve
had to let off. The car only ran a 12.075 and 53 mph. When we got back to
the pits we found that the relay for the trans brake, and the one for the
shifter were dead. Steve knew that he had spare relays, but we couldn’t
find them – must have left them home. Thanks to Simpson and Shaffer we got
replacements and were ready for Saturday’s runs.
Okay, now it’s Saturday. A new day. We have gotten rid of all the
gremlins, and we are good to go – right? We take the car up for the 2nd
qualifying run. Steve does his burnout – has a little tire shake. He
stages the car – it has fuel leaking from one of the fuel lines, then
stalls. We push him back and tow the car back to the pits. Steve tightens
the fuel lines, checks the fuel pump, and then we start the car to make
sure everything is okay. At this point, Jeff Woolard, the crew chief for
Dave Damron racing is standing on the opposite side of the car from Steve.
He says he hears a “clunking” sound from the Supercharger. NOT GOOD. Steve
and I take off the “bird” hat and look into the Supercharger. We see a lot
of gear oil, which means the bearings and the seal have died. Also, the
rotors have some scrapes on them – so basically our Supercharger is dead.
I go to tell the NPCA officials that we are broke, and done for the
weekend. I get back to the pits, and Jeff has talked Steve to putting on
the 10/71 Blower that we brought to sell on the car and continue to race.
So I go back to the NPCA officials and tell them to “Hold that thought.”
The next few hours were unbelievable. We had all kinds of help changing
the Supercharger. Rob Davis, Richard Edwards, Jeff Woolard, and several
others just took over and got things done. Wayne Sears cooked dinner for
us. Someone stopped by and said that it looked like a crew chief orgy in
our pits. I can not thank everyone enough for all the help. At 8:00 pm we
went up for the final qualifying run. The car only ran a 7.89 and 168 mph,
but we were in the show. Steve changed the pulley and the main pill, and
we were ready for Sunday Eliminations.
The first round, we had to run Richard Edwards – the guy who worked hours
on our car. We knew we couldn’t run in the low 7’s with this smaller
supercharger, but you never know, the other guy could red light, smoke the
tires, or just have a bad run, so we went up for the first round with high
hopes. The car ran a losing 7.60 and 168 mph.
We drove back to Indy, left the car and trailer at Jeff Lawson’s shop, and
flew home. Thursday 10/16 we will fly back to Indy, pick up the trailer
and head to Bowling Green Kentucky for our last race. We will race in the
7.50 class in Bowling Green instead of the 7.00 class. We should be able
to tune the 10/71 blower to run in the 7.50’s, so maybe we will have a
chance.
One last race and the season is done. Check out our sponsor –
SpecialtyToolsUSA.com, and
wish us luck.
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Car Club Night at NYIRP
September 17, 2008 |
Sally’s Night
Steve
and I belong to the Rochester Street Rods Club. The third Wednesday of
each month during the summer our club, and the Good Ole Boys Club and the
Mopar Club of Rochester meet at the local track for a drag race event.
Each club has their cars run four runs for points, but only the same # of
cars from each club get points. Any extra cars still run-but not for
points.
I
took my 1966 Mustang (289 4 speed) to the track to run with the club. I
ran 3 runs in the points runs and one run in the overflow (non points)
runs. I broke out in the non points run, but it didn’t count.
I won
the the first round of points run because the other guy went red. I won
the second round because the other guy broke out. I won the third round
because the other guy went red.
My
reaction times were TERRIBLE!!! I did not win any rounds – but because
of luck, I did not lose any either. I made points for the club- which
ended up winning the trophy , and I had a really great time. So it was a
win-win situation for me and the Rochester Street Rod Club
This
event proved to me that Steve is the best driver for our 32 Bantam
Altered. |
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Goodguys 7th Blue Suede Cruise
Summit Motorsports Park, Norwalk Oh
September 5 – 7, 2008 |
We arrived at Summit
Motorsports Park on Thursday 9/4 at 7:40 pm, about 10 minutes to late to
pull into the pits, so we parked in the lot across the street for the
night. We were first in line for pre-registration the next morning. The
booth for pre-registered vehicles opened at 7:00 am. The rain started at
7:05 and continued throughout the day.
So we had all day to
set up our pit area, eat, talk, walk around, check out the track –
everything but run the car down the track.
Saturday the weather
was good – temps in the mid 70’s and partly cloudy. We had two
qualifying runs, one at 1:00 and the other at 4:00. The first run we
went 7.123 and 181.50 mph. The second we went 7.124 and 183.94 mph. This
put us in the #6 qualifying spot.
The car is running
great in the 1st 1/8 mile, but the second 1/8 mile is BLAH!!!
Sunday morning is
cloudy and spotty rain. But the rain in done by 10:00 am.
We had our first round
of eliminations at 1:15. We had to run the Renegade car of Don Slout.
Steve had a GREAT reaction time, and the car went 7:08. We won our first
round win in the 7:00 Pro Comp I Class. I couldn’t believe it.
The next round we had
Sean DeWitt, the #1 qualifier. Steve tried hard, a little too hard, he
went .007 red – so we were done. Steve was upset with himself, but I was
really happy. Our first time in the 7.0, Pro Comp I Class, and we made it
to the semi’s.
The car ran great, the
crew did good – what else can you ask for? (Have a look at some pics from
the event...photo page).
We have decided not to
go to the Match Race Mania in Muncie, IN, so our next race with the 32
Bantam is in Kansas City – Oct 3 – 5, 2008. See you there
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Niagara
Reunion, Willys Home Run
Lancaster, NY
August 1-3, 2008 |
We
found out that Ralph, the new owner of the track, had booked “Ruby Shooz”
to play at the track on Thursday evening, so we decided to get there a day
early relax and enjoy the band. When we arrived at 5:30 pm the rain had
just ended. We went out to a local restaurant for dinner then headed back
to the track. The band was great. Ralph joined in with the band for a set
of “Elvis” songs and did a great job!
We
had all day Friday to set up our pit area and get the car ready. The temps
were in the high seventies and we had a mix of sun and clouds, but it
stayed dry all day. Steve made some adjustments to the throttle. He was
trying to adjust the launch rpm so the car would not “dead hook” and go
into tire shake as it did when we tested at NYIRP. There was a nostalgia
“bracket” race on Friday evening, but we decided to just make a test run
and see if Steve was making progress.
The
car launched beautifully. It ran 4.706 and went 128.19 mph with Steve
letting off early (he didn’t need to test that short shut down at this
point). We recorded our best 60 ft time ever on that run – a 1.0711. It
looks like Steve’s adjustments were perfect.
It
rained overnight Friday, but it was clear by 8:00 am Saturday. The temps
were in the mid 70’s with a mix of sun and clouds all day. Saturday’s
race was a nostalgia race with a 4.20 index, a 4.50 index, a 4.80 index
and a 5.10 index. The number one qualifier would be the car that ran the
closest to its index. We chose to try for the 4.50 index. Most of the
other cars were in the 4.80 index and there were a few in the 5.10 index.
Our best run was a 4.644 and 147.54 mph. We won the first round when the
other driver left before the tree was even activated, and won the second
round because that driver went red. We were going to the semi final round
when the rains started. By the time it quit, it was almost 8:00 pm. The
track officials announced that the radar showed more showers on the way,
so they called the race. The track took the total purse for each class
and split it between the remaining cars. We collected our share, and put
the car away for the night. Our Daughters and Granddaughters were in town
for the race and had a motel with a pool so Steve and I went over there,
took a shower, had a swim and hung out with the girls.
Sunday the weather was great. Temps between 72 and 78 with just enough
cloud cover to keep things comfortable. Sunday was the big race. Heads
up, pro tree, no index, no breakout – first car to the finish line is the
winner. WE KICKED ASS!!! We were the #1 qualifier with a 4.61, and got
better with each run. Our best time was a 4.54 and the fasted mph was
149. Remember “our best 60 ft time” of 1.0711? Well forget that – every
run on Sunday had 60 ft times of 1.04 and even one 1.03. The car went
straight and fast every run, and was untouchable. The only two cars at
the track that posted faster times was the Nitro Dragster and Nitro Funny
Car
At
was so great to do so well at this event, as it is the only race we have
in NY, and we had lots of family and friends there to cheer us on. We had
a couple of mechanical problems on Sunday that required some work in
between rounds. Thanks to the help of all those friends and family
members we were able to fix those problems and make the call for the next
round.
The
track announcer did a great job getting our sponsor’s name out every time
we ran, and our granddaughters passed out
Specialty Tools, Inc.
flyers all weekend.
Both
Saturday and Sunday, the NPCA cars that attended this event were the
dominate cars. If you like this nostalgia racing, you should plan on
attending one of the NPCA events. We have a link to the
NPCA website – check it out.
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NHRA Hot Rod
Reunion
Bowling Green, KY
June
13-15, 2008 |
Monday, June 9th I flew home from Indy so I could spend a few
days working. Steve headed for Bowling Green with the truck and trailer.
He had to make a slight detour to meet a guy that was selling a 14-71
supercharger. We currently have an 8-71 on the car – but not for long.
Here we go again – more changes – got to go faster.
Steve
was able to take the trailer to the track on Wednesday. Because there
were so few teams there he got a prime location. Thursday he picked me up
at the Nashville airport and we were at the track by 3:00. We took the
car to tech and as we sat in line the sky got darker and darker. One of
the techs (Bobby from Texas) took pity on those of us in open cars and
pushed us thru pretty quick. We got the car back to the trailer and
covered up before it started to rain.
We
were in ProComp A which is a combined class. A is 7.50 index B is 8.00 C
is 8.50 D is 9.00 and E is 9.50. The class runs on a handicapped Pro
Tree. So if we were paired up with a 9.50 car, that car would get one
yellow light then green THEN TWO SECONDS LATER Steve would get his one
yellow then green.
Friday morning we had our first qualifying run at 10:45. It was 88
degrees and humid. The car went 7.48 and 181 mph – first time over 180!
Because the car went under the index, we did not qualify with that run.
At
noon it started raining. Racing resumed at 2:00, and then it started to
rain again at 3:30. At 4:00 the track officials decided to call it a
day. So we went to town for dinner and spent the evening socializing.
Isn’t
it great how Mother Nature gives us these frequent breaks so we can visit
with our friends?
Saturday morning it was cloudy but dry. We made our 1st run at
11:25. At that time it was 80 and still humid. The car went 7.56 and
177. Steve didn’t want to break out again so he let off before the finish
line. That run put us in the top half of the field.
We
found out that there were only 2 cars in the Super Eliminator class. We
were told that this was also a combined class. A is a 6.50 index and B a
7.00 index. One of the two cars was in A and the other in B. We decided
to move up to the Super Eliminator B class. We had to take the car thru
tech again then make a qualifying run. We made that run at 5:30. It was
84 and still very humid. The car went 7.44 and 179 mph. The other B car
ran 7.02 on his 7.00 index. The A car ran a 6.85 on his 6.50 index. The
way we figured it the B car would be #1 qualifier, as he ran closest to
the index. On Sunday morning when they posted the race ladders, they had
the 6.50 car as #1. We asked about it and we were told that there was a
mistake – there was no B class – all three cars were running on a 6.50
index. They also had the Pro Comp class all screwed up, so Sunday was
very frustrating for a lot of people. We finally made are first (and
last) run at 3:00 pm.
We
were up against a much faster car so we knew that we didn’t stand a
chance, unless the other car made a mistake, smoked the tires, or broke.
Steve left first, and ran a 7.48 and 181 mph, but the other car went 7.09
and 191 and turned on the win light.
Even
with the class screw ups and the rain delays we had a great time, but we
have been to four races in five weeks and traveled over 2000 miles – not
counting airline miles, so we are looking forward to staying home for a
few weeks.
We
were interviewed on Speed Scene Live. Click on the link to that site and
then click on archive of past shows and select 6/17/08. Our car is shown
about 2 minutes into the video and again at about 5 minutes followed by
the interview. We got a chance to talk about our sponsor Specialty Tools
and got their web address mentioned a couple of times. You can check out
their site by clicking on their logo that is on our home page.
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Goodguys Hot Rod Nationals
Indianapolis Raceway Park
June 6-8, 2008 |
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Our
plane landed at Indy about 20 minutes late. We picked up the truck and
trailer and pulled into the track at 5:03 – registration closed at 5:00.
No big deal, we were still able to get into the pit area and set up, then
go to the registration trailer Friday morning to pick up our tech card,
wrist bands, etc. Thursday evening and Friday were sunny, hot and windy.
We had two qualifying runs scheduled for Friday and two on Saturday.
We
were called for our first run Friday at 11:00 am. It was 85 degrees and
55% humidity with a corrected altitude of 3445 ft. This was very close to
the conditions at Gateway so Steve left the tune up as it was. The car
ran 7.56 and 177 mph. That put us in the #4 spot. By the time we were to
make our second run the corrected altitude was up to 3632, so Steve
changed to a smaller pulley. This should have given us a 7.53 to 7.51
run, EXCEPT for the fact that I didn’t have the air bottle turned on.
There was enough air in the system for the burnout, but that was used up
by the time Steve staged the car. At the launch it just barely got off
the line and idled down the track. So we remained in the #4 spot.
Friday evening the NPCA group was invited to a cookout at the ARC Racing
Engine shop in Brownsburg. While we were there the black clouds moved in
and the winds picked up even more. It started to pour and then the
tornado sirens went off. It looked like the world was coming to an end
for a while, but then it got a little brighter and the rain quit. We went
back to the track
and were treated with a beautiful double rainbow. By 9:30 it started to
rain again and continued throughout the night. The next morning it was
still raining and the low spots in the pits were starting to flood. We
could tell that there wouldn’t be any morning runs, so we decided to go to
Flap Jacks – our favorite breakfast place in Indy. On our way there we
passed a McDonalds that had a “wireless internet” sign in the window.
After breakfast we went back to the track to get the laptop. It was still
raining so we might as well go to McDonalds and check email, weather &
NHRA racing results.
At McDonalds we ran into Keith “Rooman”. He told us he was going to ARC
to help Brendon Murray get his top fuel dragster ready for Sunday. On
Friday Brendon had another fire – it wasn’t as bad as last years in
Columbus, but it was bad enough to destroy his firesuit, seatbelts,
parachutes and every soft part on the engine. Because it was now 10:00 am
and still raining we decided to go over to ARC and watch. There was
another top fuel dragster there owned by a fellow New Yorker, Jim Didio,
from Auburn, NY. We talked to Jim at length as his crew repaired some
damage to that car.
It
finally quit raining around noon so we headed back to the track. We could
not believe how badly the track and pits were flooded. Steve and I walked
up to the track, at the finish line. We were standing in water up to mid
calf. They had pumps trying to rid the track and pits of water. By mid
afternoon they were making progress, but you could see that if any more
rain came it would be over. The sun came out, the breeze picked up and
things continued to dry up. The rest of the day and evening was a social
event.
By
Sunday morning four cars in our class had left due to breakage or they
thought the event would be called due to the rain. The NPCA decided to
fill in the empty spaces by moving all qualified cars up and combining
classes. This put us in the #2 qualifying spot, and that in turn would
give us the Bye run in round two – if we won round one. That would not be
easy, as we were paired up against Dave Waters and his ’40 Willys – one of
the best in the NPCA. But we did win! The car ran another 7.56,
but only 159 mph. Steve knew he was out front, and was a little concerned
about exceeding the 7.50 index so he let off before the finish line. As I
mentioned before, round two we got the Bye run. In a lone run it doesn’t
matter if you break out (exceed the index) so Steve didn’t let off. The
car ran a 7.48 and 178 mph – we need to slow it down a touch for the next
round.
Round
3 – the Semi Finals – we are up against Bob Lair in the Wild Thing front
engine dragster. Last time we raced him it was VERY close, but we won.
This time it was again very close but he won. We ran a 7.495 (broke out
by 5 one thousands of a second) and 178 mph. Bob ran a 7.51 and 182 mph.
All
in all we did great. The car was flawless, the driver excellent. Except
for some rain and my screw up with the air bottle the weekend was perfect.
Our car was filmed by Speed Scene
Live. Check them out at
www.speedsceneracing.com
and remember to check out the site
of our sponsor
SpecialtyToolsUSA.
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Muscle Car Reunion & Nostalgia Drags
Gateway International Raceway
May 31 & June 1, 2008 |

Gateway International Raceway June 1, 2008 -
Courtesy Nostalgia Pro Comp
Association
We arrived at Gateway International about 1:30 pm on Friday May 30th.
Gateway is just across the river from St. Louis. We could see the “Arch”
from the track, and we could hear the tug boats on the river. It was
sunny and hot, but we were told that a strong storm was on the way, with
winds up to 60 mph, so we should NOT set up shade tents or awnings. We
had all afternoon to set up and get the car ready for Saturday qualifying
runs. By evening the pits were packed, the clouds were rolling in, and
the wind was picking up. Steve and I sat in our lawn chairs after dark
and watched a great light show provided by Mother Nature. There was
constant lightning off to the west that was truly spectacular! It started
to rain around 10:30, and it rained hard for hours, but by daybreak it was
over. Saturday was hot (90) with 45% humidity. We did have a nice
breeze, so it wasn’t bad at all.
We made our first qualifying run at 1:21 pm on Saturday. With the high
temp and humid condition, the corrected altitude was 3120 – not very good
air, so Steve changed the pulley to compensate. The car went 7.69 and
170.21 mph, which put us in the #2 qualifying spot.
Steve made another pulley change and leaned out the fuel system a little
bit. We went for our second qualifying run at 6:43 pm. The car went 7.52
and 175.78 mph. Another car went the same ET, but with a higher mph, so
he bumped us out of the #2 spot and into #3.
Again Saturday night it rained for a couple of hours, but it was a light
rain with no wind, and again it was sunny and dry by morning. It got up
to 91 very quickly, with 35% humidity. The corrected altitude was over
3000 again. Because we ran so close to our index with the same weather
conditions the day before, we left the tune up alone.
We went for the first round of eliminations at 1:44. Steve was paired up
with a car that had been having problems all weekend, so we had a good
chance of winning the round, as long as we didn’t beat ourselves. Well,
that’s exactly what we did. Steve went RED. After both cars were staged,
the lights on the other lane flickered for some reason. Steve saw the
flash of yellow, and took off. He was really pissed at himself for
letting that flicker distract him. Then to top it off, the other car
broke before the finish line and only ran 8.09. We went 7.61 and 174.39
mph, so it could have been an easy win.
Except for the Red light loss, the weekend was a ton of fun. We handed
out quite a few flyers for our sponsor Specialty Tools USA, so maybe they
will make out better then we did.
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Match Race
Mania
Route 66 Raceway,
Joliet IL
May 17, 2008
We
arrived at the track a little after noon on Friday May 16th.
The sun was bright, the sky blue, the winds brisk and the temp was in the
low 70’s. We had all afternoon to set up and prepare the car as our first
test run was scheduled for 10:00 am on Saturday. By 5:00 the pits were
filling up, and we walked around to visit with all our fellow racers that
we hadn’t seen for months. It rained overnight, but when we woke up
Saturday morning the sun was out.
We
made our first test run at 10:39. It was sunny but very windy with a temp
of 67 and a corrected altitude of 1827 – very good air. The car launched
good, but after half track started pulling toward the wall. Steve kept
turning the steering wheel, but the car would not get back in the groove,
so he had to get out of it. Even so, the car ran 7.67 and 149 mph.
Our
second test run was at 2:13 (should have been at 1:00). It was still sunny
and windy but the temp was up to 75, and the corrected altitude was 2371
which is still pretty good air. This was a great run. The car ran a 7.51
and 177 mph – right where we need to be. Now we need to run those numbers
in the qualifying run.
We
made the 1st qualifying run at 6:05. The sky was now partly
cloudy but it was still warm, and the wind was starting to die down. The
corrected altitude was now 2289. Steve said he got his monies worth on
this run because it went from one side of the lane to the other about
three times, so he figures he went an extra eighth mile. Even with all
the dancing around the car ran 7.61 and 175 mph, which put us in the #2
spot.
We
were in the lanes for our second and final qualifying run when it started
to sprinkle. It stopped, and racing resumed. Then it started again.
This time it didn’t stop but got steadily harder. At 7:30 the event was
called. We headed back to the trailer and started loading up.
We
knew when we started out that there was a slight chance of rain, but it is
still disappointing when it happens. On the plus side – the car ran
great, we are getting a handle on the tune up, we got to see people that
we had not seen all winter, and for the most part it was sunny and warm,
which I found out was not the case in Rochester NY. This event is not
really a race, but an exhibition, so we got paid to show up and make some
runs. So even through the event was called off before the final run, we
will still get paid. All things considered, this event was a success for
the SS3 Race Team. I handed out a bunch of flyers for our sponsor,
Specialty Tools Inc., so hopefully it will be a success for them too.
Don’t forget to check out their website – just click on their logo (it’s
on the home page of this website).
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2008 Test & Tune
NY International Raceway Park
April 20, 2008 |
Finally!! Winter is over. The day was beautiful, sunny & 70’s with a
chance of a shower in the forecast, but it never happened. Steve made some
changes to the Bantam over the winter (go to the Tech Talk section of this
site and read all about it), so we were very anxious to make a few runs
and collect some data. As always when we start with a new setup, Steve
tunes the car very rich, which is slow, but safe. That combined with a
green track, we knew we weren’t going to set any records.
Steve shut the car off as soon as he made the first burnout. He had
noticed fuel leaking – it turned out to be a loose fuel fitting. We pushed
the car back, tightened the fitting, and we were ready to go. The car
launched ok, but only ran 8.30 and 158 mph.
Steve changed the pulley and the main pill to lean out the fuel system a
little, and we went for the second run. The car left the line better and
went a little faster with an 8.04 and 166 mph. There was a lot of wheel
spin after 80 ft – there is that green track. I compared the EGT’s
(exhaust gas temps) with the previous run and saw that we had made some
progress but we had room for improvement, so Steve leaned it out a little
more.
We went for our third and final run. The car leaves good again, and again
spins after about 80 ft, but goes straight and faster with a 7.87 and 168
mph. A strange thing happened at the end of the run. The parachute caught
the battery on/off switch and turned it off! The car shut off, but Steve
had enough speed to coast off the track. The bad news is that one of the
tether lines on the parachute broke, so now we have to buy a new chute. We
will send the old one back to Stroud – they might be able to fix it. If
they can we will keep it for a spare.
We made great progress at this test & tune, so we are ready for our first
event in Joliet, IL. Wish us luck, and don’t forget to check out the
website of our marketing partner, Specialty Tools, Inc. – Just click on
their logo on the home page of this site.
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