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I can't believe another drag race season has ended. Why do
the winter months last longer than the summer months? We went to 7
Nostalgia events this year plus 2 Test 'n Tune sessions. We missed 5
events due to our 6/13/07 misshap (we took out #7 rod), and it all
happened Soooo Fast!
We had our share of problems this year. The torque converter problem has
us scratching our heads for several weeks. Then we went out with a "bang"
(complete with some pretty impressive header flames) mid June. But then we
came back with a new engine, and a "let's see what this thing can do"
attitude for the remainder of the season. Of course Steve kept his tune
ups on the conservative side, as we really couldn't afford to "cook"
another engine, but we made progress every run. When we were rebuilding
the engine, Steve (with the help of Matt Shaff of Pro-Formance
Specialties) made changes that affected cam shaft timing and compression.
The "new" engine is just what Steve (and Matt) want for our car. So here
we are, mid season, with a new set-up, a new tune up, and back to square
one.
The balance of the season was a learning experience. We made progress with
every run, and ended the season on a good note. We had our best 60 foot,
1/8 mile and 1/4 times ever. The car did great on hot tracks, but not so
great on cold tracks. We continue to find out what this car wants and
needs.
We are growing, and so is Nostalgia Drag Racing. Goodguys has added at
least two new Nostalgia Drag Race events to it's 2008 season - Norwalk,
Ohio in September and Bowling Green, Kentucky in October. The Nostalgia
Pro Comp Association is continuing to grow and add events.
We are looking forward to a bigger and better 2008 season. Nostalgia Drag
Racing is growing, and we are ready to grow with it.
I will update this site with a 2008 Tentative Schedule as soon as event
dates become available.
Until then, Have a good fall, winter, Christmas, New Year, and spring. See
you all at the Track in 2008.
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NPCA Finals
Kansas City International Raceway
October 6 & 7, 2007
Our plane landed in Indy at 4:45 pm on Thursday 10/4/07 (I really like
this "jet set" racing), we hailed a taxi and arrived at Jeff's shop to
pick up the truck and trailer by 5:30. We were on our way to Kansas City,
MO by 6:00. We made it to the west side of St. Louis before we stopped for
the night. We were up early the next morning, and pulled into Kansas City
International Raceway just before noon on Friday 10/5. Quite a few cars
were already there, but we still had a good selection of pit spots. By
thie time we had our spot set up, and everything unload, the cars were
really starting to pour in. By 5:00 the pits were full, and it was
apparent that this event was going to be big.
The schedule called for a Test 'n Tune session Friday night, Open Time
Trials Saturday morning, then two Qualifying Runs Saturday evening and
Eliminations on Sunday. We decided to skip the Friday night Test 'n Tune,
and just hang out with the NPCA gang and relax.
There were several hundred race cars at this event, but it was well
organized, so things went smoothly. Our first time trial was at 11:40
Saturday. It was sunny and 83 with 64% humidity and a corrected altitude
of 3255! The car ran 7.90 and 167 mph. Steve changed the pulley for the
next run. At 3:15 we ran a second time trial. It was partly cloudy, 89
with 51% humidity and the corrected altitude was 3700. This time we ran a
7.60 - much better, but still not the 7.50 we need to run. At least we
were making full runs, and our 60 foot times were our best ever - 1.06.
Many of the other racers had a hard time with the hot track, and were not
able to go from A to B, so we were happy with the car. Our qualifying runs
were at 6:30 and 8:40 so the temps were down - 85 and 81 with lower
humidity and the corrected altitude was 3479 and 3157. The car ran 7.49
(just a little to quick) and a 7.75 (Steve let off way to early), so we
ended up qualified mid field.
Eliminations were scheduled to start at 9:00 am, but due to on and off
sprinkles we didn't get our first run until 2:00 pm. We were up against a
front engine dragster that we had never raced before (this was his first
NPCA event), but we knew that his qualifying runs were very close to ours.
The temp was 80, and the corrected altitude was 3182 - very close to the
second run last evening, which would have been in the low 7.50's (based on
660 and 1000 foot times) if Steve had not let off early, so we left the
tune up alone. This ended up being a Great Drag Race! Steve's reation time
was .043 to his .055, we ran a 7.51 and 179.53 mph (still haven't broke
180) to his 7.53 and 177.86. We got the win, and gave the fans a good
show. Steve said he could see the front wheel of that dragster out of the
corner of his eye all the way down the track!
All the classes made one round of eliminations, and that was it. The rain
started again, and never stopped. Once again, when we get the car running
great, it rains.
This was just a great event. The stands were packed. We met and raced
different people and cars. I have never had so many fans come up to us and
thank us (and the NPCA) for bring our car, and putting on such a great
show. Every run we made the fans stood up and went crazy (they really
loved the burnouts that the NPCA cars did). It was a long haul (1050
miles) and we got rained out, but we loved the track, had a great time,
and headed home with a great running car. Not a bad way to end the season.
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| NPCA Fall Nationals
Indianapolis, Indiana
September 22 & 23, 2007
We arrived at Indy early Friday September
21st. The weather was like mid-summer - temps in the high 80's, sunny and
humid, and stayed that way all weekend. The track was holding a Friday
night test and tune starting at 4:00 pm, so we decided to participate.
Steve had modified the scoop opening to allow more air into the blower,
and we had not been able to test it out, so this was our chance. As
always, when Steve changes something, he goes back to the "fat & safe"
tuneup, so the first run was a slow 7.84 ET. Steve changed the pulley, and
then went out and ran a 7.54, right where we need to be in our 7.50 index
class. We were happy with the car, and tucked it in for the night.
Saturday was qualifying day. We were to get
two runs. As I stated above, our class runs on a 7.50 index. The car that
runs the closest to 7.50 without going under, is the #1 qualifier. Our
first qualifying run, the car went 7.500. Perfect time!!! We are number 1
qualifier, and no one can "squeak" in under us. Steve left the car as is,
even though the air was much better for the second qualifying run. He
guessed that the car would run a 7.45, and he just wanted to see how well
he could predict the air/tuneup thing. He did pretty good, the car ran
7.41, our fastest time ever - it went 178.85 MPH - we still haven't broken
180 MPH.
Sunday was eliminations. We went out first
round. The car only ran 7.66. We should have changed the pulley to
compensate for the air (the corrected altitude at the time of our run was
3290 feet). The problem is, when we were called to the staging lanes, the
corrected altitude was 2740, and we had the correct pulley on at the time,
but because we were in the staging lanes for a little over one and a half
hours, the air changed considerably before we ran. So, we learned that we
will have to bring a couple of different size pulleys, the tools to change
the pulley, and the weater data station, in the tow vehicle with us. That
way we can do a little bit of last minute tuning right there in the lanes.
Every event we learn more, find better ways
to do things, and have a great time with all the other racers and
spectators at the various tracks that we go to. We left the truck, trailer
and car at a friends shop in Indy, and flew home Monday 9/24. We will fly
back out to Indy Thursday, 10/4, pick up the rig, and head to our next
event in Kansas City. This will be the NPCA Finals, and will probably wrap
up our 2007 drag racing season.
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Niagara Reunion
Willy's Home Run
Lancaster, NY
August 10-12. 2007
If you have read the "Tech Talk" section of this site, you know that the
rebuilt engine went back into the car just in time for this event. We
arrived at the track about 10:30 am Friday, and got our favorite spot in
the pits.
Again, Dick Collins and the Willy's Home Run teamed up with Lancasters
Niagara Reunion to create a HUGE three day event. The Pits were filled
with race cars from several States and Canada, and the Stands were packed
to capacity. On Sunday show cars filled every available space.
The weather Friday, Saturday and most of Sunday was Sunny with temps in
the mid 80's and humidity ranging from 31% to 42%. The lowest corrected
altitude was 2569 ft, and the highest was 3090 ft.
Friday we made two time trial runs. Because we were starting with a "new"
engine, we went back to the base tune-up, which we knew would be slow.
Then Steve made small changes throughout the weekend, leaning it out a
little bit each time. Our ET's Friday were 5.17 and 4.86 (Lancaster is an
1/8 mile track), and the MPH's were 124 and 141. The car sounded good,
handled good, improved between rounds, and stayed together, so we were
happy.
Saturday was a bracket style race for the Nostalgia Cars. We had one time
trial and went three rounds in eliminations. There were a huge amount of
cars there, so it would take many more rounds to get any money. Our ET's
were 4.81, 4.88, 4.85 and 4.80, and the MPH's were 138, 140, 133 and 145.
Based on our time trial 4.81 ET we set our "dial-in" time at 4.82. Steve's
reaction times were good so we won the 1st two rounds, then "broke out" in
the third round. The other guy also broke out, but by .0051 less then us,
so he got the win.
Sunday was the Big Race. The Four fastest cars at the track would qualify
for the "Frantic Four" and would race each other "Heads Up" with a pro
tree. The next fastest eight cars would qualify for The Quick Eight, and
compete in a bracket style race. After the 1st qualifying run we were "on
the bump" in the Frantic Four with a 4.82 ET and 145 MPH run. Our 2nd and
final qualifying run we went 4.81 and 147 mph, a little better, but not
good enough. The last car to run bumped us out of the Frantic Four, so we
ended up the #1 Qualifier for the Quick Eight.
I stated earlier that the weather was sunny most of Sunday. We were in the
staging lanes for the 1st round of eliminations when it started to
sprinkle. It quit, and racing resumed. Then it started to sprinkle again.
This time it didn't quit but started to rain - hard. By the time we got
back to our pit area we were soaked! They called the race and split the
prize money amoung the qualified cars.
This event is the only Nostalgia event close to home, so many of our
family members and friends are able to see us race. That makes this event
a favorite, and it's always a good time. We are already looking forward to
next year.
A Special

Thank You
To
Bob
Wenzelburger
for the
Fantastic
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New York International Raceway Park
Test 'N Tune
June 13, 2007
We got to NYIRP right at 5:30 when the gates opened. It was sunny and 88
degrees, but only 31% humidity, so it wasn't bad.
At 6:30 we were ready to make our first run. The car ran 8.57 and 147.58
mph. Steve made some adjustments and went up for the second run. It ran
7.70 and 168.95 mph. Again Steve made adjustments and changed the pulley.
Back to the staging lanes we went.
Steve staged the car and just started to bring up the rpms for launch. The
car made a strange noise and huge orange flames shot out of #7 exhaust
pipe, so Steve shut it off. We got the car pushed aside, hooked it up to
the three wheeler, and towed it back to the pits.
Steve did a compression test on all cylinders. All were okay - except for
#7 - it had ZERO compression. Not Good!
We had planned on leaving from NYIRP and head toward Columbus - but
instead we headed back home. No NHRA Hot Rod Reunion for us this year.
Steve started taking apart the engine the next day. He found the #7 rod
had just shattered - pieces the size of coins. The Block had monor
(fixable) damage. The Crank was good, but the Cam was junk. We had to
order new cam, rods, pistons, lifters, gaskets - you get the picture. As
long as we had to replace all those parts, Steve and Matt Saff of Pro-formance
Specialities will build a higher compression engine more suitable to our
needs.
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Goodguys 19th Hot Rod Nationals
Indianapolis, Indiana
June 7 - 10, 2007
Could could not fix the torque
converter in time for us to race at Indy, so Steve found one for sale
about 3 hours away, so off he went to pick it up. We left for Indy a
couple hours early so we could stop at Coan (just north of Indy) and drop
off the damage converter for repairs.
We finally got great weather at the Goodguys Indy event. It was sunny all
three days with temps in the high 70's to low 80's. The humidity ranged
from 29% to 53%, so the air was pretty good for racing. With the new
torque converter and good air, Steve was thinking that he just might run
in the 7.00 index class instead of the 7.50 index class.
Friday we only got 1 run due to oil downs and delays. The car ran 8.81 and
147.75 mph. Okay - we just need to lean it out a little - right?
Saturday we made two runs. The first was 7.94 and 166 mph - better, but
more adjustments needed. The second was 7.74 and 170 mph - again better,
but the car just isn't running like it should. We made more adjustments,
the car sounded better and we thought we were closing in on the 7.50 time.
Sunday, 1st round of eliminations, we ran our worst time - 8.96 and 143.54
mph - terrible! Obviously we lost.
Several times during the event we were visited by our new fan, Dani Leigh,
aka "Squirt". She is 4 years old and a die hard gear head. Her Dad had his
rat rod at the event, and Dani was having a great weekend making new
friends and checking out the cars.
We had thought about leaving the trailer and bantam at the home of one of
the NPCA members, just outside of Columbus. That way we didn't have to tow
it all the way home, then, four days later tow it back for the NHRA Hot
Rod Reunion in Columbus. But because it ran so bad we decided to take it
home and go to our local track on Wednesday (6/13) for test 'n tune. We
really have to figure out what the problem is with this car.
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Gasser Reunion
Thompson, Ohio
June 1-3, 2007
The car is back together and we headed
for the 6th Annual Gasser Reunion. The forecast is good for the
beginning of the event, but "iffy" for the end.
This track has a very bumpy shut down
area, which creates problems for fast, rigid chassis like ours. Steve
always has trouble stopping here, so he planned on shutting down early,
until he found a smooth section of track at the top end.
Friday the temps were in the mid 80's
with sunny skies. We made three runs - all slow. The tune up was way too
fat. We slowly leaned it out and showed some improvement each round.
Saturday was again sunny with mid 80's, until about 5:00 pm, then the
clouds started rolling in and the temps fell to the mid 70's. We made
four runs, again improving slightly with each run, but the car didn't
have the top end power that is should have. Steve talked to several
people, including Jim Oddy, and came to the conclusion that the torque
converter was the problem.
Our other problem is Steve never did
find a smooth path down either lane, so he will have to dial in a time
based on shutting down before the finish line. This will be very
difficult, but it's better than smashing up the car.
Sunday was cooler, cloudy and
drizzling rain, so Steve didn't have to worry about the shut down. The
event was called, and we got an early start for home, which gave us some
extra time to figure out what we had to do about that torque converter.
To see some great photos of this event
taken by Bob Wenzelburger, to to
http://rides.webshots.com/album/559379387twPRWC
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